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  1. gv_racing

    Giles' Mystery High RPM High KR

    So, it turns out I didn't know how to do a leak down test properly. I was following the instructions for good leak down testers that have an orifice between the two guages, on a cheap leak down tester that does not. Got the following results, and repeated the test a few times to ensure I wasn't...
  2. gv_racing

    Giles' Mystery High RPM High KR

    That's because you need to use the special EGR tube disassembly tool
  3. gv_racing

    Giles' Mystery High RPM High KR

    I'm not kidding when I say I've got it down to like 15 minutes on my setup. It's 7 10mm bolts, two screws, one hose clamp, and a bunch of connectors. I have a focus ST intake mani using the Damond adapter which simplifies it a lot. Gen2 as well so no PS pump. 0. get under car 1. loosen the hose...
  4. gv_racing

    Giles' Mystery High RPM High KR

    Thanks for the luck, I think I'm gonna need it lol. At this point I am convinced it is genuine predetonation knock, versus engine bay noise. Everything is pretty meticulously wire/ hose managed, and the knock is non-existent at turbo spring pressure, acceptable on my first revision (1.5 max)...
  5. gv_racing

    Giles' Mystery High RPM High KR

    It's not over yet. Replacing the injectors did make a lasting difference, but as soon as I got my next revision from Will, things started getting dicey again. Then, he sent me a followup tune with a fuel taper, which I believe will slightly lean out the mixture towards redline. This should make...
  6. gv_racing

    Giles' Mystery High RPM High KR

    Good question.
  7. gv_racing

    Giles' Mystery High RPM High KR

    Jesus christ. It was one of the injectors. Check out this 4th gear 3k-7k WOT log, that is night and day. Repeated across a few pulls. Finally I can continue the process with Will @ PD. Yay. Not entirely sure how to feel right now. Elated that my car can get tuned now. Less than thrilled that...
  8. gv_racing

    Giles' Mystery High RPM High KR

    I have a second set of recently serviced injectors on hand, so no cost involved there. I was going to try swapping them in earlier, until I found my leaking injector #3 and decided to leave them alone as I was blaming the seals at the time. I have no access to E85, just the E10 that we have at...
  9. gv_racing

    Giles' Mystery High RPM High KR

    Sigh. This is getting pretty depressing. Damond motor mounts - no improvement Swapping out injector 4 - no improvement Brand new set of overspeed seals - no improvement I honestly think my last update was a fluke. Sometimes it only registers between 2 and 3 degrees after a pull, but most of...
  10. gv_racing

    Giles' Mystery High RPM High KR

    I have made some progress on this and figure I might as well share to the class. I ran out of hair to pull and started yanking my injectors out with the intention of swapping out #4, the one which appears to be leaking from inside the connector. Last time I blasted the connector and receptacle...
  11. gv_racing

    Giles' Mystery High RPM High KR

    Thanks for your thoughts. I actually made a note in my phone to try a pull at partial throttle to see if it's load or RPM related. Will probably give that a try this evening. Also may try holding the clutch pedal in slightly during the problematic area to see if it's related to my throwout...
  12. gv_racing

    Giles' Mystery High RPM High KR

    Hey all, long time lurker first time poster. I pride myself in being a pretty good automotive troubleshooter, but this issue has been absolutely kicking my ass on my fresh engine and setup. I need the help of the MPS hive mind. ENGINE/DRIVEABILITY Year/Make/Model: 2010 USDM Speed3 Mileage...
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