SmallSon
Greenie N00B Member
Troubleshooting a friends car that has been acting up for a few months. He recently had his VVT done, head replaced, new spark plugs and new injector seals put in. Cylinder 4 spark plug used to not seat correctly due to the previous owner tearing the threads afiak. After all of that has been replaced I had him take some logs for me at WOT to check for any issues. For log 19 KR would spike to 6 for around 4k then normalize back to zero over the rest of the pull. For log 21 KR was steady in 3rd until the car was shifted to 4th at which point there was no KR at all. Any idea what would cause this type of behavior after all things mentioned have been fixed.