I have a speed6 with a remanufactured atk motor. Ever since I started breaking in the motor it has had crazy high kr at part throttle and won’t stop until I let off and 5.95 at wot consistently. Had the engine taken apart and checked and it is solid nothing is wrong. Knock sensor replaced and everything possible checked. The car ran fine prior to engine swap minus eating oil. My question is has anyone had this issue with a remanufactured motor and had their tuner fix it? And if so did it completely fix the kr? When I brought this up to my tuner prior to the new engine being pulled apart he said it was a bad idea but at this point I am out of options. I attached a wot log and a video of part throttle kr
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