DotBoi
Greenie N00B Member
My 2007 Mazdaspeed3 has been running very rich. You can drive it but I avoid to right now as it will stall at idle sometimes. My AFRs at Idle will be in the 9-12 range most of the time. Cruising is alright, except when you let off the throttle, fuel continues to enter the engine creating pops and bangs.
Mods to the car: Catback exhaust, HPFP internals, Unbranded Short ram Intake, Sure turbo inlet pipe, Aftermarket DV, Front mounted inter cooler, regular oil changes every 3k miles. 120K miles on the car.
Codes from the ECU:
P0300 Random/Multiple misfire,
P2006 Intake Manf Runner control stuck closed bank 1a,
P2178 System Too rich off idle bank1,
P2188 System roo rich at idle bank1.
The car has been running solid on a Stage 1 OTS tune for about a month, I created my own MAF calibration profile for my intake which ended up working very well for the past months.
A few nights ago driving around normally, rolled up to a stoplight and the car stalled and it has been running rich since.
A few things I've tried, cleaning the MAF, cleaning the O2 Sensors, cleaning the throttle body, re-calibrating the MAF multiple times, checked for vacuum leaks, DIY boost leak tested, and no leaks or drips anywhere that I can see. I thought maybe it would be the fuel relief valve, I noticed the Actual fuel pressure and the Desired pressure are very apart in the logs, what do you guys think it could be?
I have some Accessport logs which you can view here: https://drive.google.com/drive/folders/1vxSqElc74YZPSKeShGUbSS9QF1Wm8iky?usp=sharing
Mods to the car: Catback exhaust, HPFP internals, Unbranded Short ram Intake, Sure turbo inlet pipe, Aftermarket DV, Front mounted inter cooler, regular oil changes every 3k miles. 120K miles on the car.
Codes from the ECU:
P0300 Random/Multiple misfire,
P2006 Intake Manf Runner control stuck closed bank 1a,
P2178 System Too rich off idle bank1,
P2188 System roo rich at idle bank1.
The car has been running solid on a Stage 1 OTS tune for about a month, I created my own MAF calibration profile for my intake which ended up working very well for the past months.
A few nights ago driving around normally, rolled up to a stoplight and the car stalled and it has been running rich since.
A few things I've tried, cleaning the MAF, cleaning the O2 Sensors, cleaning the throttle body, re-calibrating the MAF multiple times, checked for vacuum leaks, DIY boost leak tested, and no leaks or drips anywhere that I can see. I thought maybe it would be the fuel relief valve, I noticed the Actual fuel pressure and the Desired pressure are very apart in the logs, what do you guys think it could be?
I have some Accessport logs which you can view here: https://drive.google.com/drive/folders/1vxSqElc74YZPSKeShGUbSS9QF1Wm8iky?usp=sharing