When I first got my speed I remember saying I wouldn't mod my car much. What a load of crap that turned out to be lol. It's been a long time coming but the big swap finally happened. Over a year ago I had the guys at Relentless Customs build me a motor. I believe it's one of the last they made before they closed shop. It's taken me a while due to life being complicated and health issues but I've recovered well and with help the motor is in and the car is running.
Build sheet as the car is now
Bnr s4 v2
Weisco piston
K1 rods
Ported head
Internally balanced
Balance shaft delete
Fidanza flywheel
Luk clutch
Cpe safe seals
Cobb 3 port
Htp 3" intake
Corksport top mount intercooler
Cnt turboback exhaust
Forge v1 bypass valve
Autotech fuel pump internals
3 bar map
Egr and tb coolant delete
I think that's it so far as the engine goes. Car has a lot of other stuff as can be seen in my Sig. Currently the car is being tuned by Freektune on 93 and next will be e33. Base tune the car is as fast as it was with a bnr s3, e33, and stock downpipe fully tuned... 330ish fwhp.
Due to recovering from chemo and wanting the car lowered onto the motor I had a shop help me get everything in and running. It hasn't been smooth lol. Ebcs wasn't wired right, slave cylinder went out, wrong clutch got installed, had a massive boost leak and I'm currently diagnosing some smoke from the exhaust, I suspect my diy egr delete might be letting coolant in the exhaust system...
Regardless I fixed all that shit and the car is finally running good and once the smoking is address the car should be close to sorted. As I tune and make more changes I'll update this thread. For now pics!

Build sheet as the car is now
Bnr s4 v2
Weisco piston
K1 rods
Ported head
Internally balanced
Balance shaft delete
Fidanza flywheel
Luk clutch
Cpe safe seals
Cobb 3 port
Htp 3" intake
Corksport top mount intercooler
Cnt turboback exhaust
Forge v1 bypass valve
Autotech fuel pump internals
3 bar map
Egr and tb coolant delete
I think that's it so far as the engine goes. Car has a lot of other stuff as can be seen in my Sig. Currently the car is being tuned by Freektune on 93 and next will be e33. Base tune the car is as fast as it was with a bnr s3, e33, and stock downpipe fully tuned... 330ish fwhp.
Due to recovering from chemo and wanting the car lowered onto the motor I had a shop help me get everything in and running. It hasn't been smooth lol. Ebcs wasn't wired right, slave cylinder went out, wrong clutch got installed, had a massive boost leak and I'm currently diagnosing some smoke from the exhaust, I suspect my diy egr delete might be letting coolant in the exhaust system...
Regardless I fixed all that shit and the car is finally running good and once the smoking is address the car should be close to sorted. As I tune and make more changes I'll update this thread. For now pics!



