Update:
@Raider and I have come to the conclusion that Lilith has some form of demon possessing her.
Per the recommendation of
@Sho I not only replaced the bar 1 fuse for giggles, I metered every single fuse in the car to ensure none of them are blown. We are good to go there, moving on.
After a few days of trouble shooting this week, I was able to discover some issues that needed addressed. Swapped some things out that... needed replaced. And have been ran through the shop manuals a few times. Some progress, but still sitting, not running properly.
Lets go:
Some
@JBR gear showed up. Wont be installing suspension items till coils and sway bars arrive, waiting on those to be in stock. I honestly don't know if i will need the spacers or not with the EVO X wheels I have, always good to have. The air dam will have to wait as well. I have some... plans that will come later.
Gonna drop some weight off that rotational assembly, because why not have some vibes to go with the DM mounts.
As stated earlier, I have been having a handful of issues, that I am assuming at this point to be wiring. After some more testing and inspecting. I am now more certain that it is the harness, I just can't seem to figure out exactly where its at. I do have an idea though.
I found one of the signal wires on my secondary o2 sensor was grounded out... I'm pretty sure that got buggered up when I put the motor in. So replaced that with another I had laying around. That helped the car idle a little better but did not fix the fueling problem I am having.
While testing after this the in tank pump finally gave out. Swapped that out with a known good pump from my MS6. Installed a new filter as well. I have this other pump that will get a new DW300 and filter once those arrive along with a new pump housing lock ring and o-ring from Mazda.
If you have never done this... I nearly had a panic attack trying to make the decision on if I drop the tank, or cut the chassis... SEND IT! Better get it over with now, than wasting the time dropping the tank knowing I am going to have to do this again very soon.
It took me about 10 minutes to cut it open and nearly an hour to get the damn ring off.
FINALLY!
Now, considering this is the original pump with 133k on it. It sat in the same 5 gallons of gas from 2015 until this last November. I would say these pumps are pretty stout. I am shocked at how little junk there was in the bucket too.
Don't forget yer lube boys
Lube up that ring for easy install and removal later
Filter was def not the worst I have seen, considering how long it sat. But, got her swapped out and flowing again to continue trouble shooting.
So I finally got fuel pressure to show up by complete accident. I swapped out the fuel pressure sensor, forgot to plug it in, and somehow, the AP read fuel pressure. I plugged the sensor back in... No pressure. This is the moment I think I have realized the car is possessed. BUT! that is good news, as this is finally some good proof to show a physical issue that has been seen and proven. This gives me a pretty good idea where to go from here. I believe the main engine harness is good, but am starting to suspect the coil or injector harness to be bad.
Until next time, Lilith sleeps more
