jesus
Greenie Member
Reaching out to see anyone has gotten some type of resolution from my current lean idle issue.
The issue is very own minded it will come and go and seems to happen at first start up cycle and with some slight throttle input for a sec or two it will come back to its desired target I've taken some logs and will leave them down below.
I've gone through and done the whole check list of test to try and get this fixed
-pressure smoke tested system for 5 mins on warm engine no leaks
-clean/swapped out with known good MAF sensor
-cleaned air filter
-double check spark plugs/gaps all good
-PRV swapped with known good one( fuel rail pressure is still high so opt fuel for idle is achieved )
-purge valve blow/suck test passed ( pause )
-has a ntk primary o2 sensor with about maybe 10-15k miles on it ( believe its reading true as the AFR is spot on at WOT )
-all ground cables/connectors good
If there is anything else that's recommended to check please let me know here's a parts list for those that want more info
Graveyard performance 4 inch intake
Bnr s4 v5 Turbo
3 port EBCS Grimmespeed
3inch Obx exhaust
3 inch catless downpipe
EGR delete
Tr10 FMIC
GFB respons bov 100% VTA
JMF V1 intake manifold with port injection
Corksport exhaust manifold
44mm Tial EWG set at 18psi spring
Bosch 3.5 bar
AEM 340lph e85 safe intank fuel pump
Auto tech hpfp internals
K-motor fuel pressure regulator base 45psi with 6AN return line
X4 ID 1050 injectors
Split second controller
Overspeed fuel injector seals
Damond stage 3 dual catch can
Damond pcv plate
Jbr mounts all around
Built Motor- 100k miles
Manly H-beam rods
Mahle 4032 pistons (88mm)
King racing rod bearings
CLEVITE main bearings
BSD delete
ARP head studs
Oem head gasket
BC0400 springs (86lbs) & titanium retainers
The issue is very own minded it will come and go and seems to happen at first start up cycle and with some slight throttle input for a sec or two it will come back to its desired target I've taken some logs and will leave them down below.
I've gone through and done the whole check list of test to try and get this fixed
-pressure smoke tested system for 5 mins on warm engine no leaks
-clean/swapped out with known good MAF sensor
-cleaned air filter
-double check spark plugs/gaps all good
-PRV swapped with known good one( fuel rail pressure is still high so opt fuel for idle is achieved )
-purge valve blow/suck test passed ( pause )
-has a ntk primary o2 sensor with about maybe 10-15k miles on it ( believe its reading true as the AFR is spot on at WOT )
-all ground cables/connectors good
If there is anything else that's recommended to check please let me know here's a parts list for those that want more info
Graveyard performance 4 inch intake
Bnr s4 v5 Turbo
3 port EBCS Grimmespeed
3inch Obx exhaust
3 inch catless downpipe
EGR delete
Tr10 FMIC
GFB respons bov 100% VTA
JMF V1 intake manifold with port injection
Corksport exhaust manifold
44mm Tial EWG set at 18psi spring
Bosch 3.5 bar
AEM 340lph e85 safe intank fuel pump
Auto tech hpfp internals
K-motor fuel pressure regulator base 45psi with 6AN return line
X4 ID 1050 injectors
Split second controller
Overspeed fuel injector seals
Damond stage 3 dual catch can
Damond pcv plate
Jbr mounts all around
Built Motor- 100k miles
Manly H-beam rods
Mahle 4032 pistons (88mm)
King racing rod bearings
CLEVITE main bearings
BSD delete
ARP head studs
Oem head gasket
BC0400 springs (86lbs) & titanium retainers

