Sho's 2007 ms3 build

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with CS tb and standard Cobb fmic piping, i occasionally get a rev hang for a second or two when coming out of gear. haven't logged it so idk what tps is doing; also haven't revised my tune since install so not sure if tweaking that will eliminate it. it isn't a consistent phenomenon and i haven't noticed any particular conditions that it seems to happen in. doesn't bug me too much, though, really.
 
Welp, shit happens and then you cry a little lol.

Coolant leak was a blown head gasket next to cylinder 4. Buddy stuck his bore scope down near the water outlet where I thought the leak was from, to see the HG is actually blown.

Oddball already has the replacement HG, and I should have head studs hopefully by next week. Just gotta figure out a few more things as well.
 

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I had the same exact issue running a similar setup, S257 turbo and 6th port on stock headbolts. Thought I had a heater hose leak at the water outlet. Turned out to be HG at cylinder 4. Stock headbolts seemed to hold to about 550 then poof.
 
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Just doing a Head gasket and back at tuning? Interested to see where you end at. Looked killer before you lost the head gasket.
 
Sweet. I have to 5858 and similar mods. Just if I can get it running. Should end up close to yours. Do your still have stock cams?
 
Did you end up using the fuel cell for PI or is it all running off the main tank?


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