Nick1150
Greenie N00B Member
Year/Make/Model: 2011 Mazdaspeed 3
Mileage: 106700
Location: Wheaton, MD
Concern: Underboosting after exhaust leak repair
DTC's: N/A
Modifications: forge bpv, aftermarket turbo inlet (just inlet, not intake), unknown muffler
ECU/Tuning Software: N/A, though I don't know if previous owner tuned the car (stock ECU)
Tuner: N/A
Is the concern intermittent? No
Can you duplicate the concern? Yes
Recent Repairs: over the year I replaced gasket between upper cat and turbo, new oem boost control solenoid from edge autosports, new aftermarket turbo inlet (couldn't afford OE), new OEM upper catalytic converter, rebuilt turbocharger from cwturbochargers (sent me a k04-881), new OE wastegate actuator.
Correction: not sure what to write here but summary of all diagnosis throughout the year: first was finding exhaust leak which was between the turbo and upper cat, pressure tested tmic, forge bpv, and tubes (plugged off at throttle body) and it all held from what I remember 14-15psi till the bpv opened, smoke tested intake and no leaks found (did plug off right before throttle body), inspected downpipe under the idea it is clogged restricting spool up to find previous owner had busted it up and it was in pieces in front of the secondary cat and found the cat mount was missing, checked vac lines at wastegate actuator and BCS to find the barbs the secure the vac lines broke off on the BCS and turbo inlet, and the original turbo had a fair amount of radial play but no axle play (still have it if needed to post photos).
Extra note, car to my knowledge isn't tuned and i don't have a AP. i do have a Bluetooth scanner and car scanner elm obd 2 app. Also I'm more of a diyer, not a car guy too. So some words and acronyms might be wrong, just let me know. Here to learn
so the journey continues, bit of a copy paste from my reddit account, tbh I didn't know about this forum till someone told me yesterday
Bought a 2011 speed 3 back on September 2021. Car was great but with an exhaust leak coming from between the downpipe and turbo. so it gets fixed but is now under boosting. Used to say 15 psi at 3k rpm wot on the gauge, but now says between 5-7psi at 3k rpm wot. It doesn't hit 15 until around 4500-5000 rpms.
Started going through diagnosis.
Pressure test tmic and rubber pipes, held pressure. Found the boost control solenoid and turbo inlet had broken vac barbs so I replaced it, OE BCS and aftermarket inlet as OE is too expensive (not intake, just inlet).
Still under boosting, so check the catalytic converter thinking it's possibly clogged restricting turbo spool up. Come to find out that it was busted and in pieces In front of the secondary cat. the previous owner did this. I bought an OEM cat and cleaned the secondary one. Still under boosting.
Eventually get a Bluetooth scantool to check everything. I find the boost gauge on the dash is reading accurately. Also my afr when trying to boost at 3k rpm drops to 10-9.5 afr which I think is pretty rich.
After that inspected the wastegate actuator and it seems to be working. Also did a smoke test instead of pressure test on intake; confirmed it's still ok.
cleaned up and relubed the bypass valve. it is a forge bpv. Also did a compression test and got these results
5/10/22
C1 155psi
C2 155psi
C3 157psi
C4 153psi
I gave up for about 7 months and recently bought a rebuilt turbo from cwturbochargers and just swapped it today alongside a new OE wastegate actuator just in case. It is still under boosting, but while attempting to boost at 3k rpm AFR is reading closer to 13, maybe related to having the ECU unplugged for a day? Also the climate control fan makes a weird sound now. I did burp the coolant with hot air on max so not sure if it just went bad or is related to turbo swap.
I can't figure this out. intake, tmic, wastegate and actuator, BCS, inlet, downpipe, turbo... Everything should be fine. what else am I missing? Why did it work fine with the exhaust leak, but now doesn't? Loved the car when I test drove it, still love it now, but it's just bringing me down. I feel like I've done everything to find the issue, but I still haven't found the problem.
https://photos.app.goo.gl/hgjah3pYJxVaRH5x5
Also a collection of photos/videos. The video of the "pull" was with the old turbo WOT once I hit 3k rpm, the honeycomb is the broken cat from before, oily turbo is old, and graph is a recent snippet from after I replaced the turbo yesterday. And most recent video is the weird fan issue after burping the coolant. Anything you need, photos just let me know, i just want to go back to the day I got it and have my full boost
Mileage: 106700
Location: Wheaton, MD
Concern: Underboosting after exhaust leak repair
DTC's: N/A
Modifications: forge bpv, aftermarket turbo inlet (just inlet, not intake), unknown muffler
ECU/Tuning Software: N/A, though I don't know if previous owner tuned the car (stock ECU)
Tuner: N/A
Is the concern intermittent? No
Can you duplicate the concern? Yes
Recent Repairs: over the year I replaced gasket between upper cat and turbo, new oem boost control solenoid from edge autosports, new aftermarket turbo inlet (couldn't afford OE), new OEM upper catalytic converter, rebuilt turbocharger from cwturbochargers (sent me a k04-881), new OE wastegate actuator.
Correction: not sure what to write here but summary of all diagnosis throughout the year: first was finding exhaust leak which was between the turbo and upper cat, pressure tested tmic, forge bpv, and tubes (plugged off at throttle body) and it all held from what I remember 14-15psi till the bpv opened, smoke tested intake and no leaks found (did plug off right before throttle body), inspected downpipe under the idea it is clogged restricting spool up to find previous owner had busted it up and it was in pieces in front of the secondary cat and found the cat mount was missing, checked vac lines at wastegate actuator and BCS to find the barbs the secure the vac lines broke off on the BCS and turbo inlet, and the original turbo had a fair amount of radial play but no axle play (still have it if needed to post photos).
Extra note, car to my knowledge isn't tuned and i don't have a AP. i do have a Bluetooth scanner and car scanner elm obd 2 app. Also I'm more of a diyer, not a car guy too. So some words and acronyms might be wrong, just let me know. Here to learn

so the journey continues, bit of a copy paste from my reddit account, tbh I didn't know about this forum till someone told me yesterday
Bought a 2011 speed 3 back on September 2021. Car was great but with an exhaust leak coming from between the downpipe and turbo. so it gets fixed but is now under boosting. Used to say 15 psi at 3k rpm wot on the gauge, but now says between 5-7psi at 3k rpm wot. It doesn't hit 15 until around 4500-5000 rpms.
Started going through diagnosis.
Pressure test tmic and rubber pipes, held pressure. Found the boost control solenoid and turbo inlet had broken vac barbs so I replaced it, OE BCS and aftermarket inlet as OE is too expensive (not intake, just inlet).
Still under boosting, so check the catalytic converter thinking it's possibly clogged restricting turbo spool up. Come to find out that it was busted and in pieces In front of the secondary cat. the previous owner did this. I bought an OEM cat and cleaned the secondary one. Still under boosting.
Eventually get a Bluetooth scantool to check everything. I find the boost gauge on the dash is reading accurately. Also my afr when trying to boost at 3k rpm drops to 10-9.5 afr which I think is pretty rich.
After that inspected the wastegate actuator and it seems to be working. Also did a smoke test instead of pressure test on intake; confirmed it's still ok.
cleaned up and relubed the bypass valve. it is a forge bpv. Also did a compression test and got these results
5/10/22
C1 155psi
C2 155psi
C3 157psi
C4 153psi
I gave up for about 7 months and recently bought a rebuilt turbo from cwturbochargers and just swapped it today alongside a new OE wastegate actuator just in case. It is still under boosting, but while attempting to boost at 3k rpm AFR is reading closer to 13, maybe related to having the ECU unplugged for a day? Also the climate control fan makes a weird sound now. I did burp the coolant with hot air on max so not sure if it just went bad or is related to turbo swap.
I can't figure this out. intake, tmic, wastegate and actuator, BCS, inlet, downpipe, turbo... Everything should be fine. what else am I missing? Why did it work fine with the exhaust leak, but now doesn't? Loved the car when I test drove it, still love it now, but it's just bringing me down. I feel like I've done everything to find the issue, but I still haven't found the problem.
https://photos.app.goo.gl/hgjah3pYJxVaRH5x5
Also a collection of photos/videos. The video of the "pull" was with the old turbo WOT once I hit 3k rpm, the honeycomb is the broken cat from before, oily turbo is old, and graph is a recent snippet from after I replaced the turbo yesterday. And most recent video is the weird fan issue after burping the coolant. Anything you need, photos just let me know, i just want to go back to the day I got it and have my full boost
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