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temp never passed 95c. I have 10 laps that session, most were slow but when i finally made a few passes i got on it. Temp was still sub 100c(212f).Got too hot then.
Edit: Hydrolock from head gasket failure maybe? How did that look?
With that said, I'm not considering reproducing a part similar to this. The integrated bearing race is a no go for me. I think replacing the hub with better material, and replacing the bearing housing with a more typical standalone wheel bearing is where I'm headed.
Made worse by what's probably a 1.6:1 rod ratio.
I would agree for sure. After taking a look at the other bores and seeing the scuff marks on both sides, this definitely suggests piston seizure which is a known concern. The OEM cast pistons run such tight P2W clearances it doesnt take much apparently.@gotovato sorry to hear about your engine woes. Might be worth looking into building a long rod K20 setup using a K24 block if you want all that RPM and reliability, probably worth a few HP on the top end too.
As for your engine failure, it's always hard to find a smoking gun when you're left digging through rubble, but in this case the telltale is in the scoring in the other 3 cylinders. The scoring is fairly circumferential, and normal cylinder wall wear basically never puts visible wear on the non thrust sides of the cylinder wall. In the majority of cases with scoring like this it's from the piston being overheated, and high RPM with a lot of ignition timing on gasoline can definitely do that, especially with a cast factory piston. This is possible without high oil or coolant temps, the only way you'd ever be able to have foresight of this failure is with an EGT probe. If you have any photos of the other pistons it may give more clues as to if that's the case here.
When I bought the car the engine was beat. 60% leak down in cylinders 2 and 3 but it actually ran great. It made no power but it ran fine and consumed no oil.Get a few miles on it to loosen up. I would be shocked it didn't come up some. Also might not even be that slow