I like to read through builds while at work, so i thought id post up my story for others to read through. Not sure if this can be considered a build or not, but figured it would be ok for me to post up here. here we have my 2011 mazdaspeed 3, purchased in late december of 2016. I bought the car after my last car was written off in a hit and run parked on the street out front my house. I purchased my speed3 off a shop owner who i have now become good friends with. the car was modified when i bought it, including a cobb RMM, cobb downpipe, auto tech HPFP internals, access port v3, cobb turbo inlet, ST coilovers, and a set of wheels i was going to buy for my last car, RPF1's 17x9 +45 with 255/40/17 bridgestone re71r tires.
super stock looking

Canadian winters, lots of snow

when i purchased the car, the show owner had a used GT3071 he was willing to do free install on if i purchased it from him. after a little thought, and seeing all the great reviews on this shops work i decided to go for it as the deal was just too good. also upgraded to an HTP 3.5" intake at this time, and installed a damond catch can.

The car also had a leaky rear main seal and part of the deal of me buying the car was that the seal would be replaced for free, and it was! took this opportunity to upgrade the clutch cause why not, free labor! went with an ACT street clutch.

the car was dyno tuned by a local shop who was well know for tuning subaru's. the tune was ok. the car was on the stock top mount, which was heat soaking very very quickly on the dyno, also the factory bpv started leaking, so boost was kept to 19psi and the car remained like that until i was able to go fmic.
living in Canada it was actually cheaper(once you factor in exchange, duties, shipping) to have fmic piping made for the car then to purchase any of the available kits.
went with a mishimoto J-line core as it was cost effective and should be able to keep up with my power goals

after the fmic the car went back on the dyno we a new forge bypass valve. i made a little extra power, up from 271whp, to 305whp and 350wtq at 19psi with the fmic and new bypass valve. At this point, the clutch started to slip. well so much for that upgraded ACT clutch. Turns out the rear main seal was leaking again. the shop replaced the rear main for me again, and this time i went with an ACT 6 puck.

after the 6 puck went in, the car remained the same for the rest of 2017. being stored over winter until it was brought out this summer, 2018. the tune it was on was OK, but the power curve sucked, so much torque but it dropped off pretty early. i knew there was more to be had, i also decided i wanted to start road racing the car alot, and that meant id like a better tune. this summer i decided to finally go with an etuner, and thats when Nishan started tuning my car, but not before all the problems i ran into after pulling it out of storage...
super stock looking

Canadian winters, lots of snow

when i purchased the car, the show owner had a used GT3071 he was willing to do free install on if i purchased it from him. after a little thought, and seeing all the great reviews on this shops work i decided to go for it as the deal was just too good. also upgraded to an HTP 3.5" intake at this time, and installed a damond catch can.

The car also had a leaky rear main seal and part of the deal of me buying the car was that the seal would be replaced for free, and it was! took this opportunity to upgrade the clutch cause why not, free labor! went with an ACT street clutch.

the car was dyno tuned by a local shop who was well know for tuning subaru's. the tune was ok. the car was on the stock top mount, which was heat soaking very very quickly on the dyno, also the factory bpv started leaking, so boost was kept to 19psi and the car remained like that until i was able to go fmic.
living in Canada it was actually cheaper(once you factor in exchange, duties, shipping) to have fmic piping made for the car then to purchase any of the available kits.
went with a mishimoto J-line core as it was cost effective and should be able to keep up with my power goals

after the fmic the car went back on the dyno we a new forge bypass valve. i made a little extra power, up from 271whp, to 305whp and 350wtq at 19psi with the fmic and new bypass valve. At this point, the clutch started to slip. well so much for that upgraded ACT clutch. Turns out the rear main seal was leaking again. the shop replaced the rear main for me again, and this time i went with an ACT 6 puck.

after the 6 puck went in, the car remained the same for the rest of 2017. being stored over winter until it was brought out this summer, 2018. the tune it was on was OK, but the power curve sucked, so much torque but it dropped off pretty early. i knew there was more to be had, i also decided i wanted to start road racing the car alot, and that meant id like a better tune. this summer i decided to finally go with an etuner, and thats when Nishan started tuning my car, but not before all the problems i ran into after pulling it out of storage...
Last edited: