gotovato
Greenie Member
had a bit of weekend.
it started with me wanting to install my oil cooler...which of course the sandwich plate has gone missing. cant find it anywhere so thats VERY ANNOYING.
anyways,
this weekend i did the rear endlinks as they were indeed making noise. OEM fomoco endlinks lol, 87k miles on them. they dont owe me anything.
next up tackle my leaking oil feed. this thing has been pissing for weeks now. its bad. what a pain to get at but it wasnt as bad as i expected.

i changed both washers top and bottom. started the car and it was pissing. like bad. ok. tightened it up more, still leaked but much less...ok. tightened the ever living hell out of it. stays dry now!
so slow day at the shop. fixing oil feed and endlinks. time to go home.
leaving to shop is about 15 minutes of side streets then the highway. took my time getting to the highway. once on the on ramp i always give it the beans...well this time....
SMOKE SCREEEEEEEEEEEEEEEN. oh fuck. welp. lets go wot again...
SMOKE SCREEEEEENNNNNNN AGAIN!!. Well fuck
smoke was coming from under the hood from under the car from everywhere
i pulled over as soon as i could, since the car was running and driving fine and this is what i had the pleasure of being met with,

i basically started crying immediately and started planning out my next steps. maybe panicked too soon. i cleaned this shit up best i could, and went at it. i did about 40 wot pulls on the way home, 3-4, 2-3-4, ALL of 4th to 7500rpm.
no problem. car was fine. 0 issues. what im thinking happened and only because i remember so clearly but i checked my oil before leaving the shop. some oil dripped off the dip stick around the dip stick tube holder and on the JMF there is material there and it was oily so after putting the stick back in (or maybe not putting the stick back) i wiped up the oil around the dip stick tube, my guess i lifted the dip stick out a bit with the cloth and that was that.
welp, i did many many pulls on sunday after cleaning up as much of the oil as i could. got the car super hot(it was 99f outsitde) and oil was just dripping down everywhere lol. this sucks.
Car was happy though. i did my usual array of stupid moron pulls giving it literally ALL OF IT. car was fine. didnt care. making good power even in the heat.
so now what?
well...i spoke to Matt of damond, and ive got a new catch can check valve coming as i suspect mine is starting to fail(noticed it hissing during a boost leak test). ive also got the damond PCV plate on route, and a single vented can. Matt went over everything on the phone with me basically giving me the run down on why i should have at least ONE vent somewhere, specially being on a built motor. so i will be running the below setup going forward,

i also need a transmission as my 5th gear no longer likes to shift from 4th at 7500rpm...or really anyting over 4000rpm. itll go, but crunch crunch. guess when i install my 6 puck again ill swap in my spare trans and have this one rebuilt. ah well. how it goes i guess. 5+ years of literally getting the beans everyday and some stuff is now tired. im not mad, its just annoying everything is failing this year lol. damn
it started with me wanting to install my oil cooler...which of course the sandwich plate has gone missing. cant find it anywhere so thats VERY ANNOYING.
anyways,
this weekend i did the rear endlinks as they were indeed making noise. OEM fomoco endlinks lol, 87k miles on them. they dont owe me anything.
next up tackle my leaking oil feed. this thing has been pissing for weeks now. its bad. what a pain to get at but it wasnt as bad as i expected.

i changed both washers top and bottom. started the car and it was pissing. like bad. ok. tightened it up more, still leaked but much less...ok. tightened the ever living hell out of it. stays dry now!
so slow day at the shop. fixing oil feed and endlinks. time to go home.
leaving to shop is about 15 minutes of side streets then the highway. took my time getting to the highway. once on the on ramp i always give it the beans...well this time....
SMOKE SCREEEEEEEEEEEEEEEN. oh fuck. welp. lets go wot again...
SMOKE SCREEEEEENNNNNNN AGAIN!!. Well fuck
smoke was coming from under the hood from under the car from everywhere
i pulled over as soon as i could, since the car was running and driving fine and this is what i had the pleasure of being met with,

i basically started crying immediately and started planning out my next steps. maybe panicked too soon. i cleaned this shit up best i could, and went at it. i did about 40 wot pulls on the way home, 3-4, 2-3-4, ALL of 4th to 7500rpm.
no problem. car was fine. 0 issues. what im thinking happened and only because i remember so clearly but i checked my oil before leaving the shop. some oil dripped off the dip stick around the dip stick tube holder and on the JMF there is material there and it was oily so after putting the stick back in (or maybe not putting the stick back) i wiped up the oil around the dip stick tube, my guess i lifted the dip stick out a bit with the cloth and that was that.
welp, i did many many pulls on sunday after cleaning up as much of the oil as i could. got the car super hot(it was 99f outsitde) and oil was just dripping down everywhere lol. this sucks.
Car was happy though. i did my usual array of stupid moron pulls giving it literally ALL OF IT. car was fine. didnt care. making good power even in the heat.
so now what?
well...i spoke to Matt of damond, and ive got a new catch can check valve coming as i suspect mine is starting to fail(noticed it hissing during a boost leak test). ive also got the damond PCV plate on route, and a single vented can. Matt went over everything on the phone with me basically giving me the run down on why i should have at least ONE vent somewhere, specially being on a built motor. so i will be running the below setup going forward,
i also need a transmission as my 5th gear no longer likes to shift from 4th at 7500rpm...or really anyting over 4000rpm. itll go, but crunch crunch. guess when i install my 6 puck again ill swap in my spare trans and have this one rebuilt. ah well. how it goes i guess. 5+ years of literally getting the beans everyday and some stuff is now tired. im not mad, its just annoying everything is failing this year lol. damn




